Mathias Agopian a97ead75db fix [3369027] Sensor.TYPE_ROTATION_VECTOR is unstable and returns NaNs when running slowly
The cut-off frequency of the lowpass filter was too high
for the sampling rate used by DELAY_NORMAL.

Now we use the same filters used for the gravity vector
(cascaded biquad at 1.5 Hz)

Change-Id: Iac290a716cc47a78337a8f0e45b103e49b4d9d78
2011-01-19 15:32:38 -08:00
2011-01-11 22:54:10 -08:00
2011-01-07 15:21:54 +08:00
2011-01-18 15:25:32 -08:00
2010-11-04 16:17:52 -07:00
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